Raucous Kenwood Chef A701a

A noisy Kenwood Chef A701a gets a gearbox rebuild.

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This Chef had been sleeping quietly in a kitchen cupboard for some time before being woken up to make cake mixtures once again.  The owner had owned the mixer for many years from new and was sentimentally attached to it.  I fully sympathise, they’re great machines.  It had been used many times in the past and then packed away as new machines came and went.  Having decided that there was still a place for the A701a, it was fired up.

The owner didn’t remember it being quite as noisy and wondered if something was wrong with it.  She got in touch and brought it in to the workshop.   After listening to the mixer at varying speeds, we agreed that perhaps it was a bit noisy and that further investigation was required.

 At this stage I must confess at this repair has been on the bench for a long while..!

I think the A701 is my favourite Kenwood Chef product as it’s very elegant, beautifully proportioned and almost over-engineered.  It comes from a time where built-in obsolescence was a swear word.

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FixItWorkshop, Oct’17, Kenwood Chef, A701a,

On with the problem.  After disconnecting the gearbox by removing the drive belt, I checked the motor for general wear and tear, the brushes and speed control mechanism and I concluded that it all seemed OK and working smoothly.  The gearbox however did seem a bit noisy when turned manually, nothing hideously graunchy, but a little rough.  To be honest, it would have probably survived, but I wanted to open up the gearbox to make sure that it was as it should be.

Whilst removing the Chef’s casing around the gearbox, I’d noticed traces of grease around the joints and various power take-offs.  All models seem to do this to an extent, but this one seemed to be quite bad.  Closer inspection revealed that some of the grease had escaped out of the seal between the two halves of the gearbox casing.  Opening up the casing revealed that the grease that was left had been pushed to the corners of the space within the gearbox and that the gears were a bit dry, this was probably the root cause of the noise.  The planet wheel that drives the beater was also bone dry.

Luckily, there are plenty of suppliers who can supply rebuild kits for Kenwood Chef gearboxes, including new gears and grease.  The gears in this seemed serviceable, but it seemed very sensible to replace the lubricant with the correct 130g of Kenwood gearbox grease, which is food safe.  I used ‘Kenwood Chef Restore’, an eBay seller and the kit was a reasonable £10.99, including P&P.  The kit included the main gearbox grease, white grease for the planet gear and sealant for the gearbox casing.

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FixItWorkshop, Oct’17, Kenwood Chef A701a, repair kit from Kenwood Chef Restore, eBay.

Before replacing anything, the first job was to clean out all traces of the original grease which had gone very sticky and was contaminated with general wear.   The first pass clean involved using paper toweling, followed by water and detergent, before a final clean with brake cleaner, which removed the last few traces of grease and dirt.

With the gearbox refilled and resealed making sure the spacers were re-fitted to the correct parts, the drive belt re-fitted with just enough slack, the gears sounded much sweeter with the final parts of the casing reassembled.  One last point to note is that I used silicone sealant on the blender attachment power take-off plate in replacement to the one fitted, since the original seal was well past it (see below).

As a finishing touch, I replaced the existing machine feet which had turned to mush with replacements from Sussex Spares (eBay shop) for a very reasonable £2.70, delivered.

The Chef was now ready to prepare cake mixtures again.

Cost of new machine: £300 and up.  Cost of replacement parts: £13.69 (plus my time).

 

Hillbilly Compact Light / lite Golf Trolley going nowhere (motor needs new brushes)

A frustrated customer brought this ‘stationary’ mobile golf trolley in to the workshop recently.  He’d replaced the control unit along with the hand controller.  The battery was also new, but the trolley wouldn’t respond to the controls.

A systematic test of the wiring revealed no problems and power was getting to the motor OK.  However, with the unit switched on, every now and then, the motor would make a noise, a faint hum.

This indicated that the motor, a Lemac 65178-101, was trying to do something.  A few searches online revealed that the Hillbilly Compact is no longer made and parts, including the motor, are hard to obtain for reasonable money, this is a shame as the unit is only just over 10 years old.

The customer likes this particular model due to its lightweight and compact folding ability.  New ones are several hundred pounds and usually heavier.

Since the rest of this trolley is serviceable, it seemed sensible to have a go at a repair.  With the motor removed, the cause of the fault became clear.  The commutator was heavily blackened and scored and one of the brushes had burned away, probably due to the heavy weight the trolley had lugged around a golf course.

Being realistic about spend on parts, I thought it would be a good idea to order some replacement brushes from Amazon.  These brushes will come from Hong Kong via Sourcingmap (an excellent source of hard to get parts) and I will let you all know how I get on with the repair.  The motor’s back-plate is available online for just over £15 plus P&P, but I like to repair the problem, rather than waste components that still work.

More to come… I expect you can’t wait.

One the new brushes are fitted and the commutator cleaned, I hope the motor will spin once again.

20/08/17

The brushes arrived and fitted perfectly.  Time will tell if the brush material stands up to the tough punishment of lugging golf clubs across a green, but for £2.41, the repair was worth a try.  See video.

Here are a few photos of the motor refitted to the golf trolley.

Cost of a replacement golf trolley is circa £300+; The cost of the parts to repair this one; £2.41.

04/09/17

Well after some ‘light use’ the owner of the golf trolley contacted me to report that it had failed again, my heart sank!  After a few hundred yards, the trolley came to a halt, which caused some amusement on the fairway…

After testing all the wiring again, I suspected the motor once more.  After removing the motor, I saw that one of the brushes had stuck to the carrier, hmm, interesting.  It seemed that the brushes I’d fitted had run ‘hot’ and started to deteriorate prematurely, which was a shame.  When I ordered these to ‘fit’ this motor, there was always a risk that they wouldn’t last as long, since I didn’t know the exact specification for the motor- I took an educated guess, which turned out to be wrong!

I looked online again and discovered another set of brushes available for this Lemac motor, from http://www.lambeggolfshop.com, for a very reasonable £8.48, including delivery within 48 hours. I didn’t find these brushes the first time, so I must have used different search criteria, this time.

The motor now spins freely and it’s fitted back to the trolley and I hope this time, it makes a round to the 19th hole!

 

Bissell Powerlifter Pet noisy roller beaters

Now, some of you will remember that I’ve written about a similar issue before, but I think it’s worth covering again as often, complete replacement items need to be purchased, which can be costly.

This Bissell Powerlifter Pet vacuum cleaner had snapped a belt, due to an obstruction in the roller/ beater area and while the casing was open to replace the belt, I removed the beater to see how smoothly it turned.  It was noisy.

Seemingly, Bissell will only supply a complete unit for around £30, with shipping, so given the overall value of the machine, it seemed sensible to have a look at the noisy component on the bench.  The bearing housings, located at each end of the roller, come out easily and with some careful manipulation, each bearing can be removed.

On this unit, both bearings were dirty and dry.  Now, I could have replaced them with a generic bearing, but in the spirit of thrift, I decided to clean the bearing races with brake cleaner and then repack with high-melt-point grease.  When reassembled to the roller/ beater, it ran very smoothly and was much quieter, once re-fitted to the vacuum cleaner.  Job done.

 

Pump, ready for the dump

This asthmatic car tyre pump came in to the workshop with little going for it.  The owner had been very close to throwing it away when he came across my website.

This AirMan pump is designed to be plugged in to a car’s cigarette lighter socket and provide quick and convenient car tyre inflation.  This one was dead.

On first inspection, the fuse was OK, the switch seemed to work and all connections seemed sound, when tested with a multi-meter.

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FixItWorkshop, Worthing, May’17 AirMan Car Tyre Pump, repaired

Off with the cover…

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FixItWorkshop, Worthing, May’17 AirMan Car Tyre Pump, repaired- cover removed

When the motor was removed from the cam driving the piston, the bit that drives the pump, it spun freely when power was applied, using a battery in the workshop.

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FixItWorkshop, Worthing, May’17 AirMan Car Tyre Pump, repaired- gear wheel

Seemingly, the centre spindle was protruding far beyond it’s specified reach, causing the pump connection rod to it it during rotation.  Why?  To be frank, I wasn’t sure. I can only surmise that the vibration and heat had caused the flywheel/ toothed drive to slide outside of specification.

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FixItWorkshop, Worthing, May’17 AirMan Car Tyre Pump, repaired- washer

There appeared to be room for a small washer to take up the excess space, so I fitted one I had lying around.

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FixItWorkshop, Worthing, May’17 AirMan Car Tyre Pump, repaired- pump now in line with washer

The washer, once fitted, allowed the flywheel/ toothed drive to sit ‘square’ in-line with the pump.

Once resembled, the pump ran freely and was ready to inflate, once more.

Cost of a new pump, circa £20.  Cost of the washer, circa 5p.

Dyson DC33 repaired in the workshop

Conked out Dyson DC33

This Dyson presented with a pretty terminal case of ‘no go’.  The owner had run this relatively new machine in to the ground with little maintenance so it was little wonder what happened next.

Whilst in use, the machine spectacularly went bang and tripped the main fuse board of the house.  The noise and following smell was quite something I was told.

The owner had nearly rushed out and bought a new machine and was budgeting between £300 and £400 for a replacement.

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FixItWorkshop, Worthing, Feb’17. Dyson DC33 motor replaced

I was glad I could help since I was fairly certain I knew what the problem was without seeing it.  After giving the cable, switches and casing a visual inspection, it was time to delve deeper.  The filters were in poor condition and the general smell of it indicated that overheating had been an issue, probably leading to premature wear on the motor.

With the motor out, the true extent of the damage became apparent.  Both motor bushes had worn away to nothing and part of the brush holder had broken up inside the motor, probably while it was running, causing the noise.

I suspect that the owner had ignored the warning signs of burning smells and occasional cutting out (as the thermal overload circuitry performed its fail-safe role).

Being only a few years old, the owner had a couple of options; either replacing the faulty part with a genuine Dyson replacement (a very reasonable £40) or pattern motor kit with filter pack for under £25.  The owner chose the latter on the basis of the machine’s age and the fact that both filters in the machine were also ruined.

The job took an hour, including testing before the machine was back performing its cleaning duties once more.

A note to all vacuum cleaner owners (that don’t take bags):  Keep your filters cleaned every couple of months or so.  Your machine will last much longer if you do.