This cheap and quite frankly nasty DVD player came in as a dud unit. No lights on, nothing. To be frank, not even I thought it would cost in to repair it, since the owner told me it didn’t cost more than £20 in the first place.
Never mind, off with the cover and a quick poke around with the multi-meter revealed no power coming from the transformer within the unit. This converts high voltage from the mains to lower, safer voltages for the player. On this DVD player and many others I’m sure, the internal processes are broken up in to ‘cards’. On this unit, there’s a power card, a logic card for the motor drive and a video card for the picture. Closer inspection of the (cheap and horrible) power card revealed several faulty components, which had failed catastrophically. At first glance, I suspected that the cost of replacing individual components wouldn’t cost in and that sadly, this DVD player might be headed for the bin.
Fear not! With the power of Amazon, I was able to find a generic suitable DVD power card via China that fitted, with a small amount of wiring for £5, delivered. Job done.
This asthmatic car tyre pump came in to the workshop with little going for it. The owner had been very close to throwing it away when he came across my website.
This AirMan pump is designed to be plugged in to a car’s cigarette lighter socket and provide quick and convenient car tyre inflation. This one was dead.
On first inspection, the fuse was OK, the switch seemed to work and all connections seemed sound, when tested with a multi-meter.
Off with the cover…
When the motor was removed from the cam driving the piston, the bit that drives the pump, it spun freely when power was applied, using a battery in the workshop.
Seemingly, the centre spindle was protruding far beyond it’s specified reach, causing the pump connection rod to it it during rotation. Why? To be frank, I wasn’t sure. I can only surmise that the vibration and heat had caused the flywheel/ toothed drive to slide outside of specification.
There appeared to be room for a small washer to take up the excess space, so I fitted one I had lying around.
The washer, once fitted, allowed the flywheel/ toothed drive to sit ‘square’ in-line with the pump.
Once resembled, the pump ran freely and was ready to inflate, once more.
Cost of a new pump, circa £20. Cost of the washer, circa 5p.
This Kenwood Chef developed a nasty little problem. The failure smelled expensive and the Chef even puffed out some smoke when it began to fail, it would operate, but noisily and badly, so it to the workshop it had to go.
It was in decent overall condition and has loads of accessories, so definitely worth saving since a new one is over £300 new.
Since the speed control circuitry is a common failure on models of this age, it seemed sensible to start there. On this unit, access wasn’t a problem and the issue was quickly diagnosed. Both capacitors had failed (spectacularly) and one of the resistors had become weak by about 20 Ohms or so. Repair kits are readily available online for those who are willing to save these excellent machines, so after removing the faulty components, new items were fitted.
Another little annoying problem with the Chef, was the main drive belt. It was intermittently rubbing the main plastic body of the unit, making a horrible sound and melting some of the casing (only cosmetic). The motor mounting spacer had compressed on one side causing the belt to not run correctly. This was fixed with a small washer to correct the belt’s alignment.
With a little bit of grease, WD40, Brasso, contact cleaner, repair kit and washer, the whole job took a couple of hours (including fettling time) and cost me under £8. Definitely worth the effort considering the price of a replacement Chef.
Here’s a picture of the new components fitted in situ…