Ultimate Speed Battery Charger from Lidl, on standby

Battery charger repaired at the workshop

Advertisements

My in-laws have an ornament on their drive, in the shape of a 2001 MGF roadster.  I say ornament because it’s fairly stationery, all of the time.  Even so, it’s battery gets topped up once in a while and the engine turned over when the urge presents itself.  Because the car isn’t used, the battery’s only means of charge is via a plug-in charger, my father-in-law occasionally hooks up.

IMG_5316.JPG
FixItWorkshop, March’18, Ultimate Speed (Lidl) Battery Charger.

The battery charger in question is an Ultimate Speed (Lidl brand) universal battery charger.  They’ve been on sale in the UK for a number of years at the £15 (approx.) mark.  They’re really good value as they allow ‘smart charging’ of car and motorcycle batteries without the risk of damage at a fraction of the price of the ‘big brands’ or a replacement battery.

However, this charger decided that it wasn’t playing anymore and refused to offer it’s charging services when recently connected to the MG’s flat battery.  On it’s way to the great bin in the sky, I managed to divert the charger via the workshop.

Once connected to the mains, the standby light illuminated, indicating something was actually happening, but upon connecting the low voltage side to a battery, making a charge selection via the single push-button switch, nothing changed and the whole unit remained on standby.  Pretty annoying.

Luckily, I have the triangular screwdriver required to undo the six screws that hold the (IP) ingress protected casing together.  Triangular screw heads are annoying and pointless as they prevent, in my opinion, people with a basic tool set having a go at a repair like this.  If you do fancy getting one of these tools, they are easily available on Amazon and eBay.

On with the fix.  With the casing opened up, my first port of call was with the switch itself.  Past experience has taught me to 1; start with the easy stuff and 2; these push to make switches fail all the time.  They’re in everything from door bells to cookers at the moment and when faulty, make the most expensive item and expensive paper weight in the blink of an eye.

To test the switch, I connected the charger to the mains and hooked up the low voltage end to a battery and simulated the button push switch by shorting out the switches connections on the circuit board.  Hey presto, the charger worked perfectly, every time.  The switch either needed repairing or replacing.

Because I’m a skin-flint, I opted to see what could be done with the present switch.  With care, these switches can be prised apart, using a sharp knife and the insides cleaned.  I took the switch apart which revealed nothing more than slightly corroded switch surfaces.  I can only assume that the product’s bold IP rated claim is a little over exaggerated and that some damp had wriggled its way to the switch and mucked it up.  With a cotton bud and switch cleaner, the switch surfaces scrubbed up like new and I re-assembled the switch lever and securing plat using a soldering iron to re-melt the plastic nubs holding the switch together.  No one would ever know it had been in bits.

With the circuit board returned to the housing, all six screws done up, the charger was back to rude health once more and ready to tend to the stranded MGF.

Nearly flaming 1986 Yamaha XT600 Ténéré

Beloved Yamaha XT600 Ténéré nearly goes up in smoke.

I’ve had my beloved Yamaha XT600 Ténéré for about 8 years and have deliberately kept it away from these pages as I’m always doing something to it.  It could have its own website with the amount of time, not to mention money and effort I’ve spent on it.

IMG_20180128_141128
FixItWorkshop, Jan’18, Yamaha XT600 Ténéré.

This story is note-worthy as it’s a lesson for me and others who ride and maintain old bikes!

I don’t use the bike that much at the moment, but I always keep it ready for the road, just in case I get a chance to take it out.  Whilst doing a few checks recently, I decided to fire it up and get the oil pumping around the engine, so that things don’t seize up.

The tank was pretty full (over 20 litres) and upon opening up the manual fuel valves, giving it a bit of choke, the engine fired-up on the second crank.  It sounded quite sweet.

However, after about 30 seconds, I heard ‘running liquid’ before smelling the intense scent of super unleaded.  Looking down, I was standing in about 2 pints of fuel, on the wooden shed floor with a hot exhaust casually burning the fuel that was dripping on to it.  Nasty.

I won’t repeat what I said, but suffice to say, I hit the bikes’ kill switch virtually instantly.  I shut the flowing fuel off and wheeled the bike out in to the open air.

After several cups of tea, I found the cause of the problem.  The small fuel feed pipe which runs from the float chamber to the main jet on the carburettor had failed causing the leak.

When I bought the bike, I thought I’d changed all the fuel lines, but I’d missed one, quite an important one as it turned out.  It goes to show that even enthusiastic mechanics make mistakes.

The cost of the repair was £1 for a new piece of fuel hose, but the point of this story is:  If you have any petrol-powered things, especially old motorbikes; don’t run them in an enclosed wooden space.  Always run them outside.

Porsche Boxster leaky window seal

A little water leak repair on a Boxster.

Not strictly a FixItWorkshop blog article really, but hey!  It’s a cheap fix.

My beloved 2003 Boxster developed puddles in the umbrella holder on the passenger side (RHD car) when it rained hard.

The window was adjusted correctly and the door aligned properly, but when it rained, water ran down near the door mirror, under the seal, down the door card and in to the umbrella holder area.  Water leaks like this, especially on the passenger side (RHD car) are a real problem on the Boxster, since the cars’ ECU is mounted on the floor on that side and is big £££ to replace/ repair if it fails.

Seemingly, the door seal rubber on the car adjacent to the door mirror area had worn and become slightly porous and was allowing water to get in between the glass and seal.

New door seals are very expensive and to prove the issue, I applied a small trace of tap (faucet) silicone grease to the area to restore the wax-like finish, the seal should have to seal properly.

This has fixed the problem for now.  The door seal is worn and will need replacing in the long-term, but for now, this is a very cheap fix.

 

Pump, ready for the dump

This asthmatic car tyre pump came in to the workshop with little going for it.  The owner had been very close to throwing it away when he came across my website.

This AirMan pump is designed to be plugged in to a car’s cigarette lighter socket and provide quick and convenient car tyre inflation.  This one was dead.

On first inspection, the fuse was OK, the switch seemed to work and all connections seemed sound, when tested with a multi-meter.

IMG_3604.JPG
FixItWorkshop, Worthing, May’17 AirMan Car Tyre Pump, repaired

Off with the cover…

IMG_3598.JPG
FixItWorkshop, Worthing, May’17 AirMan Car Tyre Pump, repaired- cover removed

When the motor was removed from the cam driving the piston, the bit that drives the pump, it spun freely when power was applied, using a battery in the workshop.

IMG_3588.JPG
FixItWorkshop, Worthing, May’17 AirMan Car Tyre Pump, repaired- gear wheel

Seemingly, the centre spindle was protruding far beyond it’s specified reach, causing the pump connection rod to it it during rotation.  Why?  To be frank, I wasn’t sure. I can only surmise that the vibration and heat had caused the flywheel/ toothed drive to slide outside of specification.

IMG_3596.JPG
FixItWorkshop, Worthing, May’17 AirMan Car Tyre Pump, repaired- washer

There appeared to be room for a small washer to take up the excess space, so I fitted one I had lying around.

IMG_3597.JPG
FixItWorkshop, Worthing, May’17 AirMan Car Tyre Pump, repaired- pump now in line with washer

The washer, once fitted, allowed the flywheel/ toothed drive to sit ‘square’ in-line with the pump.

Once resembled, the pump ran freely and was ready to inflate, once more.

Cost of a new pump, circa £20.  Cost of the washer, circa 5p.

Incontinent Porsche Boxster (986)

A slight departure from my usual ramblings about white goods and other domestic appliances in this entry.  Outside of The Workshop, I’m a keen petrol head who loves to tinker with cars and motorbikes and my own car was suffering from a recent bout of coolant incontinence.

Like me, most owners of these cars dread anything like this happening as it usually means big money.

The leak only happened when the car cooled after it was was run up to temperature and was evident in the area under the oil filter housing.  Luckily, the leak wasn’t serious and was repairable with a 10mm spanner, washing-up bowl and 4000 grit sandpaper.

Here’s a little video which I hope will help other Boxtser owners.